So after an 8 month break from updating this thread a lot has changed.
The car was dropped back onto it's wheels to take to MOT ready for French Car show.
I tried to start it next day and it wouldn't go. After a bit of trial and error with flat batteries and dodgy wiring bodges by the previous owner I had a disaster.
A small puff of smoke from the Adaptronic signalled the end of it's life. :ak:
This prompted a bit of a teddy throwing session before I got on to Scoff and ordered the newer Adaptronic 420D to replace my old 420C.
It arrived a few days later and I proceeded to rewire the engine loom as a number of things were different between the two.
The car started but had serious starting problems and once running was obviously on 2 cylinders.
After a lot of head scratching, back and forth messaging to Scoff and a number of new parts, (Ignition coilpack, leads, plugs, crank sensor and second rewire) we eventually found out the reason it had been so hard to start. The previous owner had removed the F7R Megane (60-2 tooth pattern) and uprated Megane clutch and had fitted a standard GT Turbo (44-2) flywheel and standard GT Turbo clutch. No wonder the ECU couldn't run properly as it was trying to read an incorrect tooth pattern.
Gavin and I replaced the flywheel with a spare Megane one I had and fitted a 182 clutch that Gav had in his spares pile.
Once all back together and the adaptronic adjusted the car ran on all 4 for the first time since I got it back.
I am thinking that the previous owner may have had problems running it after the change and couldn't sort it so gave up and that's why it was parked up for 3 years.
Oh well, at least all the ignition components were now brand new as well as ECU and wiring loom.
All this happened over a period of a few months due to work and family commitments as well as all the diagnosis time.
On the test drive it was obvious that things needed tweeking including the exhaust, gear selection and handbrake.
So, back under the car to sort things out and a few patches of rust were spotted which would likely have failed the MOT.
This led to a full interior strip out to ascertain the extent of the rot. It was a LOT worse than I first thought................