So I found a little water leak on the end of the head, a chap at work had some gasket paper so I removed the plate and old gasket, cleaned it up and made a new one with some added hylomar blue. hopefully that sorts it. Managed to get all 4 bolts out without snapping them. Made myself a new King lead using some spars I had kicking about and then swapping the boots around. Set the point gap though I need to look into why the dizzy seems loose whilst clamped up. Not much else done. Tomorrow I will set the valve clearances and hopefully have the spark plugs. Fingers crossed it starts well and gains some lots performance.





